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10110185 TESTING ENGINEERS, INC. 2811 Teagarden St. 510-835-3142 510-834-3777 fax San Leandro,CA 94577 800-660-3142 San Leandro • San Jose • Martinez INSPECTION REPORT Week Ending: 1/21/11 PROJECT#53857 TYPE OF INSPECTION: Reinforcing Steel Placement/ Concrete Placement/Epoxied Dowels PROJECT: --- PLACE OF INSPECTION: Bubb 8(Apple) Jobsite 10231 Bubb Rd. Cupertino,CA Permit# 10110185 DATE 1/17/11 1/18/11 1/19/11 1/20/11 1/21/11 HOURS 4 8 4 4 8 INSPECTOR M.Ardizzone Reported to Duane of DPR Construction at the jobsite as requested. 41 1/17/11 .3•Z V1 Inspected the placement of reinforcing steel at six(6)brace frame footings and one(1)exterior footing. 1/18/11 Monitored loads arriving at the jobsite for correct mix and proper slump. Inspected placement operations and vibrating procedures. Performed 1 slump test(4-Y2")and cast 1 set of compression test specimens(4 each),Sample# 236988,for Concrete Mix# 3EFEC9Q1 from Central Concrete Supply Co.,(specified strength 3000 psi,slump 4")for concrete placed at six(6)brace frame footings and one(1)exterior footing. Total cubic yards placed: 90. Inspected the placement of anchor bolts and reinforcing steel for the above. 1/19/11 Inspected the placement of reinforcing steel at column base footing on line 1.25 from E.5 to F.S. Inspected predrilled holes for proper diameter and depth. Observed the cleaning of holes and the injection of Hilti Hit Re 500 SD epoxy(exp.7/11). Witnessed the proper insertion of one hundred sixty(160)#4 reinforcing steel bars,30"in length, embedded 3"on lines G from 2 to 3.5,4 from C to D,1 from D to A and 4 from A to B. This report can be reproduced only in its entirety unless written permission from TEI is obtained. Page 1 of 2 Bubb 8(Apple) 10231 Bubb Rd. Project No.: 53857 W/E: 1/21/11 1/20/11 Monitored loads arriving at the jobsite for correct mix and proper slump. Inspected placement operations and vibrating procedures. Performed 1 slump test(4)and cast 1 set of compression test specimens(4 each),Sample#236998,for Concrete Mix#3EFEC9Q1 from Central Concrete Supply Co.,(specified strength 3000 psi,slump 4")for concrete placed at electrical trench in-fills. Total cubic yards placed: 12. Inspected the placement of reinforcing steel for slab on grade and the above. 1/21/11 Monitored loads arriving at the jobsite for correct mix and proper slump. Inspected placement operations and vibrating procedures. Performed 2 slump tests(4",4")and cast 2 sets of compression test specimens(4 each),Sample#236997,236999, for Concrete Mix #3EFEC9Q1 from Central Concrete Supply Co.,(specified strength 3000 psi,slump 4")for concrete placed at slab on grade, slab in-fills between lines A and B from 1.5 to 3.5,C.25 and D from 1 to 4,at F.5 and G from 2 to 3 and footings on line G at 3.5 and 1.5. Total cubic yards placed: 100. Inspected the placement of reinforcing steel for the above. The preceding work was,to the best of my knowledge,in compliance with approved plans and specifications,including revisions by engineer. Reviewed by: _ Davi ippero Special Inspection Division Manager 1cc: Apple Computer Inc./C.Kealey,The CRE Group DPR Construction/J.Spielman City of Cupertino/Bldg.Inspection Dept. This report can be reproduced only in its entirety unless written permission from TEI is obtained. Page 2 of 2